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92LS400...s/c?

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Posts posted by 92LS400...s/c?

  1. dang, that happened to my mom's car and my car when I changed the water pumps on ours, hers a 94 mine a 92. It turned out on her I forgot to plug the MAF sensor back in(I know, dumb) but it ran almost exactly the same and also I had put the passenger side rotor on backwards. So maybe you should check those but since you said it ran good for a while it might not be. My car the 92 what had caused the rpm signal 2 code was i guess some water got in the coil on the top, thats the rpm signal 2, the coil went bad so i replaced that fixed that code; then, the knock sensor was when i had reran the knock sensor i didn't hook it back under the coil which caused the serp belt to rub it and eventually cut the wire so i had to go to pick n pull and get a new after that the idle went back to normal on both cars and ran fine. So to recap check the MAF sensor, make sure the rotors on correct, check if knock sensor wire is cut and replace coil if needed

  2. well its almost a year later and my water pump went out again; so I replaced the spark plug wires and rotors and water pump again and what do you know the hesitation has gone away. the car runs smooth as ice again. I suspect the problem was the rotors, however on occasion at driving highway speed the check engine light comes on and says it's running lean...but it doesnt really seem to be. I wonder what that could be?

  3. Oh, well when I removed the fuel filter I would prime the pump to see if it was working and a nice flow of gas came out so it works fine.

    As for the distributor cap and rotors, I think its been a while since they've been replaced; but, I might have replaced them when I changed the water pump witch was about 6 months ago now. I can't really remember I'll have to check on those.

  4. How much money did you spend "deleting" the EGR ??

    like $15, I cut out some brackets for the EGR pipe and and the valve, than capped all the vacuum lines. I just copied the kit from lextreme; better than $100 for a piece of metal and bolts, and a lot better than $200 for a whole new valve. I noticed when I took the valve off there was a very large amount of "soot" I guess you'd say layering the intake manifold where it connects. I tried my best cleaning it but it was pretty tough and I didnt get it all off.

    and when you say "did I check the pump itself" you mean the EGR valve? if so than yes I did; it was stuck closed...

    So could it be that EGR build up getting lose and making something else mess up?

  5. my check engine light came on and it said it had an egr malfunction so instead of replacing i deleted it since i am poor, the check engine light is now off; my vaccuum lines all seem to be in good condition and the car only hesitates when cold now. could it be the ports from the egr are so dirty on the intake that its still some how messing with the performance?

  6. recently my LS has been hesitating at 2100RPM usually when I'm going around 60-70MPH, and i don't know why its doing it. I just replaced my water pump about a month ago and the car has been hesitating since. So i replaced my plugs with platinum plugs and replaced the plug wires, pcv valve and cleaned the throttle body i also got a new air filter. None of these things have fixed the hesitation, does anyone have any ideas what it could be? :wacko:

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