DougJohn2, it is doing much better. I had to have the head gasket replaced and have the head surfaced. That fixed the oil/coolant leak. At the same time I had to have the head/throttle body cleaned of Carbon. It was plugged up real bad. I replaced the 3 components of the EGR system and that fixed the CEL. However, it still knocked real bad even on 93 octane. When they pulled the head off, the mechanic showed me the EGR port on the intake. It was totally plugged with carbon.
Now that I have all of this done, it drives great. Even runs on regular gas like it is supposed to do. For the first time, I am enjoying this truck. Now that I have practically restored it, I will keep it for a very long time (as long as not many more surprises).
Thanks for asking as it was a real mess for a while.
Andrew