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Posted

UPDATE: 

For anyone who needs a permanent solution for this problem, I'm making and selling these parts in a complete repair kit, on eBay and at my website http://www.bluemooseengineering.com

I've redesigned the part a bit...nice strong radius sweeps at the bottom and a much nicer finish. The part in the original post was hand machined using a vertical mill. These parts are being made on a Haas VF2 so the finish quality is a lot nicer. 

image21.jpg?w=700&h=&crop=1

image122.jpg?w=700&h=&crop=1
 

Here's a .pdf of my installation instructions. This includes detailed steps and pictures for door panel removal as well:
https://bluemooseengineering.files.w...eplacement.pdf

======================================================

Hi everyone,

I've been lurking around the Lexus forums for a little while, and have come here for information off and on for many years. My father-in-law is a die-hard Lexus owner (I'm a Honda/Acura guy myself but I still really like Lexus) so over the years I've helped him fix his cars many times and the forums have always been very helpful.

FYI - I just posted this same write-up over at Club Lexus earlier today. 

Our most recent adventure involves the now-infamous broken passenger window clip debacle. Our repair of this has gone so well, and I have seen nobody on any forum provide a similar solution, so I thought I'd share what we did and how we did it.

First a little bit about me. I have a background in Quality and Engineering, and mechanical design and fabrication. I have worked at a few glass and plastics manufacturers in Southern California over several years, so I may be uniquely qualified to work on this specific problem. Currently, I'm the Quality Manager at an industrial flat glass manufacturer. We specialize in glass machining and specialty flat glass parts for aerospace, scientific, medical, display, and lighting.

So here's a summary of what I know about this problem based on my reading. I'm providing this in case you are just discovering that your car has this problem, and this is the first thread you've happened upon. For the veterans on the forum, please feel free to correct any of this information:

  • The earlier models of the 5th gen ES350 suffer from a chronic failure of the plastic clip that joins the window regulator to the window
  • This seems to affect the passenger window only
  • This seems to affect the first three model years (2007-2009) - is this true?
  • The only real solution so far has been to replace the entire piece of glass, which comes with new clips pre-adhered to the glass - not a bad fix but also fairly expensive and now, most often outside of warranty coverage
  • It is alleged that the clip was redesigned on later models and on replacement parts so the failure does not recur - can someone confirm this?

We went through the process of reporting the problem to the Lexus dealer, and attempting to negotiate a free or discounted repair. They were not completely inflexible and agreed to fix the problem for the retail price of the part (sparing us the labor charge). This was still going to cost ~$400 and we thought we could do as good of a job for less $$$.

Before I share our repair, I just want to comment on the nature of the failure.

I have seen several posts in several threads that theorize about the root cause of the failure and how to fix it. Nearly all of this speculation is probably wrong. Some deride the use of a plastic clip - there is nothing inherently wrong with using molded plastics for these applications. This part is exposed to very little stress linearly or laterally so a properly designed molded piece should not fail...we know this because most cars use a similar system and do not fail chronically.

Someone else commented that a hole should be drilled in the glass and the regulator arm joined directly to it. It's not that this couldn't work, but its important to think of holes in a piece of glass as defects, or potential defects. Drilling a hole in a piece of glass forever compromises that piece of glass, and for a moving part, should probably be avoided. I have seen this design fail many times so its not surprising that the industry has moved away from it. It is more costly and more likely to fail intermittently and unpredictably.

Also the term "waterjet" was used...just an FYI - water-jetting glass is really a no-no. The initial blast of abrasive-filled water causes substantial chipping and flaking at the entry site and is not the proper way to put a hole, or cut any shape, in glass, unless it is going to undergo substantial further machining.

So why does this part fail? Well not surprisingly, I believe it can be traced back to the design of the part, and keep in mind that this is just a theory. Take a look at the pictures below:

80-failure_1_88f5f42d4f8170dcd0afe14e827

80-failure_2_f825ff97f58e3e042371c64b361

First, you'll notice that the point of failure, at least on this part, is a very thin section at the bottom of the U. This does not defy expectations..there's absolutely no reinforcement in that area...it's very thin.

I believe that since the window is curved, and travels on a curved path, and because the window regulator is straight, and travels up and down quite linearly, that at the extremes of the window's travel, there are very slight lateral forces being applied to the clip. The part was never designed to handle these types of forces repeatedly.

That, combined with thermal cycling of a fairly extreme nature (depending on where you live) and the rate at which the passenger window is actually cycled up and down, leads to a failure of the plastic part. To me, this is actually good and bad engineering. It would be very difficult to overcome the problem of curved window and path/straight regulator. So the fact that the smallest and presumably cheapest part in the assembly fails, is in many ways good..you wouldn't want those forces being transferred through to the glass (although I don't foresee heat tempered glass breaking that easily).

You could argue circularly for hours about whether the motion design or the part design is the true root cause. But, since the motion design would be very difficult to overcome, and the part design fairly easy to overcome, the burden of fault lies with the part. It's just weak.

I have not seen the redesigned part from Lexus but I imagine that it contains bracing or is thicker in the area highlighted by the red triangles in my illustration above. Perhaps someone who has received a replacement dealer window can confirm?

Either way, if you find that your car is suffering from this failure, what are you to do? Well most people will have to just suck it up and pay for a replacement window. We took a different path.

I have access to machining capability and expertise so I decided to leverage that and just create a new clip. We machined this from aluminum (didn't record the grade - not particularly important for this application):

80-new_clip_1_012d970f55ebf7ef8c7a338c5a

Side-by-side comparison


80-new_clip_2_5dfb895f22e6a7b5a6bdf25735

Another side-by-side


80-new_clip_3_d9ee483222b005da6a0af5bd8b

Grooved to increase surface area - this mimics the design of the original part


The new part came out beautifully and I couldn't wait to get it installed.

The first step was to remove the door panel and speaker. There are numerous how-tos for this everywhere so I'm not going to repost all of that. Once the door panel was removed we dropped the window regulator low enough to access the site of the broken clip.


80-image8_1c08e676b4be0908fcc6663d8ab137


The next task was to remove the old adhesive. This is a fairly soft rubberized adhesive (more on that in a bit) so it scrapes off very easily using a fresh razor blade:


80-image10_595b8ead34889da0a861dac5d29bc


We did our best to get the area as clean as possible. It's tough to reach some spots. Once we removed as much of the adhesive as we thought we could, we wiped the surface with isopropyl alcohol (you could use acetone or equivalent solvent):


80-image11_806b7c97122251983167d8fa4e99c


Once the area was clean we gave the part a test fit:


80-image12_233934bd1336a7601d4dc18f166e3

Looks great and it kind of clips right into place. It's obvious that the fitment is perfect. 


Then we removed the part and filled the gap full of adhesive. I spent a LONG time selecting an adhesive for this and finally settled on a 3M Urethane-based windshield adhesive for a number of reasons:

  • This adhesive is designed specifically for adhering glass to coated and uncoated metal substrates - perfect - that's exactly what we are doing
  • The adhesive in this application acts as both a damper and as a bonding agent, securing the part to the glass and absorbing vibratory forces transferred through the vehicle frame to the door and to the regulator so it needs to be thick and rubbery
  • The adhesive should have a fairly short work time and a high strength bond - this has an ~15 minute work time and a 72 hour Lap Shear strength of 550psi - our bondline is going to be thicker than that used for the lap shear test, but the takeaway is that this is a tough application-specific adhesive

The adhesive we used is 3M part number 08693 and is available off the shelf at O'Reilly/Autozone/Pepboys/et al for about $15. We used less than an ounce of it but you can just plug the tube and keep it for something else:

MAJOR NOTE: WEAR RUBBER GLOVES - just touching this adhesive spreads it around like wildfire and it doesn't come off your skin easily - ask me how I know pat.gif


80-image15_1ef047170d97a6a8a001ff4191919


Once the entire gap is filled in with adhesive, I used one finger to press the regulator arm backward to make space, and using my other hand, slid the clip up onto the glass in the approximate location. I let the regulator arm come forward to its natural position, then moved the clip into place centered over the bolt hole:


80-image16_f249733a9dc4a7f9e9041637521f7

A lot of adhesive will be forced out. This is good. This is exactly what the factory job looked like. in this case, more is better! 


I smeared a little extra on and around the part just as a precaution. It looks messy but that's okay! Nobody's going to see it anyway:


80-image17_009789228d7bf959ec322e3e29cfb


The only thing left to do was wait for it to cure then test it and put it all back together. We waited way past the actual cure time (24 hours) of the adhesive and went for about 60 hours before testing. Check out the attached video for our "test". The window operates totally smoothly with no noise at all. I call this a tremendous success.

Additional note: For some reason taking apart the passenger-side door panel and control disabled the drivers-side switch for that window, and also the auto function on the passenger-side window switch. Maybe someone here knows more about this than we do (I believe it has something to do with "pinch protection"?) but we were able to get things working again by using the down +5 seconds and up +5 seconds trick.

So what do you think?

Honesty and transparency are important to me so I might as well just come out and say that I've been toying with producing and selling these. This whole thing started as me helping out my father-in-law, but the more I read, the more I realized that there are probably a lot of people in need of a more affordable solution for this problem.

I'm making a few more parts and creating a CAM file then I'm going to talk to a machine shop about actual production.

I admit that I didn't read the fine print so I want to say that my intent is not to break forum rules. I'm here to share my work openly with the community, and to perhaps sell some of these parts. If this requires vendor status and paying my due to the forum operators, I'd be happy to discuss that. Mods - please PM me if you want to talk about this.

 

Window Test.MOV


Posted

Hi Rich,

Thanks for sharing this mod with us...definitely a cost saving over the original item.

Best bet is to email Steve to discuss going forward with your idea

Regards  Trevor

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